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Car
54 Update |
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8/19/10 Unfortunately
the late Wednesday night attempt to get the car on the track did not work
out. We got the car together and
running in the early hours of Thursday morning but when we got to the track
the car did not sound right. We found
that last week’s issue caused more damage to the motor than we knew about and
we were unable to race this week. |
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8/12/10 We
had some trouble with the handling in the first practice but with some help
from the 55 team we were able to improve.
We did not have a heat race so we started 19th of 24
cars. We worked our way up to 14th
with only about 5 laps the go the car shutdown and would not re-fire. We ended up with a 20th place
even though we did not finish. The
motor needs a lot of work for next week and my son is sick therefore we may
not get the car ready in time for Thursday’s race. Hopefully things will work out and we can
get on the track. |
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8/5/10 Rained
Out- Rescheduled to Sunday 9/26 |
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7/29/10 The
day started out bad but we ended up with a decent finish. In the first practice the car did not have
the power still but in the second practice we found out why. I was running side by side with the 91 then
all of a sudden the car just lost even more power. It turns out a lifter broke. Luckily we had a late start for our
feature. We were able to pull the top
end of the motor apart and replace the broken lifter before the start of the
feature. Because we did not make the
heat race we started dead last of 22 cars.
We quickly passed a few cars then went back and forth with the 00, 38,
15 and 46. There were many cautions
and wrecks, but we were able to stay out of all of them even with a couple
close calls. In the end we finished
with our best this season in 11th.
It turns out we did not get all the pieces of the lifter out of motor
and over the weekend found that the pieces caused some damage to the
motor. Unsure of the severity of the
damage, we decided the replace the motor with our original that we just
finished putting back together.
Hopefully it will have the power we need this week. |
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7/22/10 Practices
were not great but not too bad. Our
times were not as fast as the past few weeks but not horrible either. The car went great through the entry and
good through the middle but when on the gas the car was loose. With the lack of a heat race this week and
shortened practices we had trouble tuning the car in. We started 16th in the
feature. We were faster through the
turns than the cars we were racing against but the lack of momentum off the
turn made it difficult to finish a pass.
We had a few close battles throughout the race with the 46, 45, 02 and
38. We ended up with a 13th
place finish, not bad considering the poor handling of the car. |
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7/15/10 Practice
started out great! We were running the
fastest time we ever have. We were
only a little slower than the top runners.
Then we started 3rd in the heat, the car started off loose
and we dropped back to 8th.
The car came in near the end and we were faster than the 6th
and 7th place cars that were battling for position. In the 4th turn on the last lap,
we made a bold move to go inside three wide to take 6th. This put us on the pole for the
feature. Something happened to the
car’s power and we quickly dropped back after 2 laps. There was a caution and we were able to
come off the track to check the car out.
We made it back before the end of the caution but had to start
last. The car was no better with power
but the handling was great. We were
able to make a few quick passes but then the excitement got to me. I started overdriving the car and caused a
wreck which took out two innocent cars.
On the restart the car filled up with smoke from a tire rub and then
in turn 1 the tire blew out causing me to spin and hit the wall. Check out pictures from the day here. After a lot of work we have the car ready
for the 22nd when the PASS super late models will be there. |
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7/8/10 It
was another decent week for us. We
still are not where we want to be but the car is getting better. In the practice we broke a belt but we got
it fixed quickly. In the heat we started
on the pole but fell backwards after a couple laps. We started the feature in 16th
and with a last lap pass finished 14th. The car stayed consistent throughout the
race but still does not have the same power as the top runners and we still
have some work to do on the handling.
Some adjustments to the cam may give us the power we need off the turn
for next week. |
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7/1/10 Finally
we are headed in the right direction.
The motor had some power but it needs to be tuned to get more power
off the turn. We are back to running
the lap times we were running last year at our best. The practices and heat went well with no
issues. In the feature I had trouble
getting around the 02 car and we lost the rest of the pack. once I got around the 02 I was not gaining
or losing the pack. All we needed was
a caution but it never came. We
finished 13th, a big improvement from the past few weeks. Hopefully with some adjustments this
weekend we will continue to improve. |
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6/24/10 We
got some tips from the 55 team on our setup for this week and we were
excited, thinking this was the week for our luck to turn around. We tried something different from what we
ever had and in practice, as expected, the car felt different. It took a little getting used to. The car was
still a little off but is something we can work on to get better. In the second practice, we broke a brake
rotor in the 3rd turn but I was able to keep it off the wall. We got it fixed before the race. The feature went caution free but our car gradually
got slower and slower down the straight aways as the race went on. It turns out the car was running on only 7
cylinders. We found out later that one
of the lifters fell apart. Maybe next
week our luck will turn around. |
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6/17/10 The
motor was in and we were ready to race but still needs some adjustments to
get all the power out of the motor that we can. We were not as fast as usual but were able
to race. At the start of the feature
the lack of power was apparent but once it hit high RPMs it wasn’t too
bad. After 8 laps there was a caution
and, when shifting, the car would not go into gear. Unfortunately, we had to get pushed off the
track and did not finish the race. The
shifter linkage came apart. |
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6/10/10 This
would be probably the only week out of the season that would be happy to have
rain on a Thursday. We found out that
the car ran out of power because of a broken piston. We have been working on an extra motor that
was not completed. My father put a lot
of extra time in this week to try to get the car ready for today. I am not sure if it would have been ready
if the rain did not pass though causing a rain out. The new motor will be ready to go in the main
car for next week when the Modified Racing Series (formally the True Value
Modified) is in town. Our makeup,
along with the modified shoot out, from 6/3 will be on 6/24. |
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6/3/10 The
practice seemed to go well, we were back to running our typical lap
times. We started on the pole in our heat
race but the car lost all the power it had in practice and we got passed by
everyone. Before our race the rain
started and the track could not be dried.
Our feature next week will be based on today’s feature. |
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5/27/10,
50 Lap Feature After
our changes throughout the week, the car was still low on power. We started on the outside front row in the
heat race but dropped to third quickly, shortly after we had our first
caution. On the restart the leader
“tried to pay the second place car back” by pushing him into the wall on the
front stretch. His car bounced back
inside right at my passenger door and I sup hitting the wall taking us out of
the heat. With a quick response from
the track welder, we were able to bend the rear rails of the car back away
from the tire and get the torn bars welded up. Luckily we had no suspension damage. We got the body riveted and taped up in
time for the 50 Lap feature.
Unfortunately we started in the rear but we slowly gained spots but
the lack of power was hurting us on the straights. We finished 16th out of a 25 car
field. The night was a little
disappointing but considering the abuse the car took in the heat, I am
pleased. We have a lot of work ahead
of us this week end to get ready for next Thursdays TNT featuring the Tour
Type Modified Shootout! |
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5/20/10 The
start of Thursday Night Thunder.
Things again did not go as planned but we managed to finish the
race. Practice showed that we had some
mechanical problems so in an attempt to repair them, we over compensated for
the feature. The car was low on power
out of the turn in the feature causing us to slip back from the start. We limped through the race to finish one
lap down. Unfortunately it was one of
our worst finishes, but we know what we need to do for next week’s 50 lap
feature. |
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5/13/10 We
ran into a little bad luck after practice on 5/6/10. We found out that the motor has a major
issue. We took the backup car to
practice today and found a setup we can work with for next week’s TNT. The
start of the season is one week away and we are excited! |
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4/11/10- Ice Breaker, Day 2 Things went a little smoother today
but we did not get the finish we were hoping for. We started 17th and finished 17th
out of 23 cars. The car slowly lost it’s
handling as the race went on and once again we went the entire race without a
caution. Some good things came out of
the weekend. 1) The car came off the
track in one piece. 2) We know what we
need to work on for the start of Thursday Night Thunder in May. 3)
We had a lot of fun. 4) Our new
spotter loves the race track.
4/10/10- Ice Breaker, Day 1 Things started out a little rough
for us. We drew numbers for starting position
in the heat race; I pulled a 48 which meant I was starting in the back of the
pack. In the first practice rounds, we
had an oil leak which we could not find.
Finally we found it and got the car dialed in. In the heat race, a car spun in front of me
without a caution causing me to fall back behind the pack. Just as I was catching the pack, another
car spun in front of me causing me to lose the pack once again. This time I was not able to catch back
up. I will start tomorrow in 17th
place. 4/3/10 – Practice We took the backup car today to get
the bugs worked out and the get it handling better. Now, if we need it this season, it will be
ready. 3/27/10 - Practice First time on the track since
2009! Although it did not go as well
as we would have liked, the practice sessions helped us with what we needed
to know. What do we need to work on to
improve the cars for the Ice Breaker?
We had time to get both cars on the track and found some minor issues
that need to be fixed. We hope to make
sure that both cars are ready if needed, one is ready for the next practice
and we are trying to have the other ready before then also. The 10th and 11th is
coming fast and we can’t wait to kick the season off. |
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